Sunday, May 5, 2024

I Didn't See That Coming

Now that the engine is happily rebuilt and running, I've started planning for what I need to do to get it back in the boat.  This is a huge task that brings the phrase "How do you eat an elephant" to mind.  The answer is of course: "One bite at a time", so the first bite in the process is to get the tarps and part of the frame off to make overhead room for hoisting the engine back in.  

Unfortunately, the deck isn't wateright at this point and that needs to be done before the tarps come off, so I guess the real first bite is: Getting the deck watertight.  The hatches and most of the deck equipment are well sealed and I have re-plumbed the scuppers, but the chainplates are out of the boat and all 7 chainplate assemblies and underdeck tie rods have to be reinstalled.  On paper, it seems like a simple job, but reality always gets in the way.

I pulled the chainplate assemblies out of storage and took them apart to see if anything needed replacing. I should note that these are not your standard stainless or bronze bar chainplates that fit through a slot in the deck and bolt to a bulkhead. These are NavTec chainplates which consist of a deck plate with 2 bolts that go through the deck and connect to an aluminum block which connects to a tie rod which connects to a bulkhead mounted chainplate.  

In theory, they are a nice solution because you don't necessarily need a bulkhead located directly where the chainplate goes through the deck.  They also only have 2 bolt holes that go through the deck and are easier to seal than a slotted bar with a rectangular hole in the deck.  However, what I found when I took apart the chainplate assemblies was less than ideal.

Most of the NavTec chainplate system is made up of nitronic 50 which is essentially a super corrosion resistant stainless steel (better than 316) and a yield strength nearly twice that of 316 stainless.  All of these parts look brand new and will be re-installed as is, but there is an aluminum backing block that ties the above-deck chainplate to the tie rod and on 4 of the 6 blocks, I found serious corrosion that would need to be addressed in several ways.

First, the backing blocks would need to be replaced, but I wasn't able to find a source for replacement so I decided to digitize the blocks and have new ones machined.  I haven't used CAD in years so I was pretty rusty but my son has a Autodesk Inventor license and he helped me get up to speed on the software and once I got the hang of it, I was able to get it done without issue.  To make sure my design was within tolerances of the originals, I 3d printed one of the blocks in PLA to make sure everything fit and once I was satisfied (I did a few iterations), I sent the designs off to a machine shop to CNC them out of 7075 aluminum with a hard anodized coating.

The second, and more concerning issue was why the blocks corroded in the first place. The only way that could happen was if water was making its way down from the deck to the blocks mounted underneath.  A quick inspection of the deck revealed that the core underneath the chainplates on deck was crushed (probably from overtightening the tie rods that attach to the bulkheads).  I was surprised that an area as crucial as the chainplates would have a plywood core and not solid glass, but I shouldn't be surprised by that sort of thing anymore.  The Niagara is a well built boat and a lot of thought went into isolating through hulls from the core, but I feel that they missed the mark with deck fittings.  Time to get to work.

When I re-cored the decks on my Alberg 35, I epoxied in 9 layers of 1708 biaxial cloth where the chainplates went through the deck so no core could be exposed. While this was effective, it was part of a bigger, messier job so I didn't have to be careful about the surrounding deck surface.  For this job I wanted to do something similar, but without having to re-core the whole deck.  After some discussion on several online forums, I settled on the idea of creating oval inserts with flanges made of G10 plate that would replace the existing deck top skin and core material.  The inserts would be .25" proud of the deck and would create an 'island' around each chainplate that would help keep water out of the holes.  I drew up a schematic of what I wanted it to ultimately look like and then did a few 3d prints to make sure my measurements were correct before I started cutting expensive G10 plate for the actual installation.  Next time I'll go into the gory details of cutting holes in deck and epoxying the 'island' inserts into place.




 

  




Sunday, March 31, 2024

A Big Milestone - A Fitting Day for a Westerbeke Resurrection

So after 3 weeks, I finally got my pump back from the injection shop on Friday.  It was all rebuilt, shot blasted and painted. Hopefully it would work, but unfortunately I had a bunch of family Easter stuff going on for most of the weekend so I had to put it on hold until this afternoon.  When I finally freed up, it was go time.

It only took about 10 minutes to re-install the fuel injection pump and timing shim, and getting the governor tie rod and spring back on the pump rack in the little hole in the side of the block was surprisingly easy because I had tied on a piece of fishing line onto them so if I dropped them inside the case I could retrieve them easily.  Because I've done it several times already, the rest of the fuel system was easy, but time consuming (2 hours). 

Once everything was back together and everything checked and re-checked, I rolled the engine over to the shop door, grabbed a pail of water and starting battery and hooked up the ignition panel. My son came over to the shop and we checked to make sure power was going to the glow plugs and fuel pump. It took a bit of time to get the high pressure side of the fuel system primed, but once it was, it fired right up and sounded great.  We ran it through the throttle range with no issues other than adjusting the throttle idle setting (a bit too low).  Also notable was that there was zero smoke and there was good water flow out the exhaust.  

I'm ecstatic that this milestone is complete. My original plan was to get the rebuild done 'over the winter', so technically spring has started and I missed my deadline, but I'm still calling it a win.  Of course there's still a ton to do to get the motor back in the boat and installed, but this was a big one.

Here's a link to the YouTube video if you want to hear it purr: It's Alive!

Thursday, March 14, 2024

While I wait

With the injection pump at Diesels Fuel Injection Services for a rebuild (should be completed next week) and the weather still a bit too cold to work on the boat itself, I decided to tackle rebuilding the propeller. With previous boats I've owned, I've only had 2 blade fixed props, but Velorum came with a MaxProp classic which is a 3 blade automatic feathering prop.  I've seen them before on other boats at the yard, but never really paid attention or gave them a second look.  I'm not convinced that a slowish cruising boat needs a feathering prop but I'm sure I will appreciate the additional power a 3 blade will deliver and not be concerned with the drag that a fixed 3 blade would have on performance.

Anyway, the prop was in a box in several pieces and covered in grease and barnacles, so I wanted to clean it up to assess if it needed to be serviced.  I started by degreasing all the parts and doing a rough scrub to get as much old marine growth off as I could.  

After the first round, it really didn't look any better than when I started except there was less grease. 'Less' is the keyword here because even the industrial strength grease remover I was using didn't seem to do much other than spread it around.  Close to a roll of paper towels and more degreaser finally proved effective and I was finally able to handle the parts without my hands turning black.  

Next, I tried a brass wire brush to get the rest of the barnacles off and finally resorted to a wire wheel, but it still looked pretty sad.  After a little online research, I picked up a gallon of vinager and soaked all the parts in a bucket overnight.  That seemed to loosen up the remaining barnacle 'roots' and I was finally down to a mottled brownish bronze finish. 


I felt like I was finally making some progress (albeit slow). My wife suggested I use Bartenders Helper to get it shined up.  Apparently, it's a powdered form of oxalic acid with some sort of abrasive in it.  Once again, I'll admit my wife is brilliant, that stuff works great.  Just shake some on the part and scrub it with a wet sponge and it works wonders. After a few rounds of that stuff, it looked great (at least the pieces did).  

Now it was time to put it all back together and hope all the pieces were there.  I found that PYI Inc is the distributor and service center for MaxProp in addition to the very popular PSS dripless shaft seal (I'll be installing that once the engine is back in the boat).  They have a great site and even though the MaxProp Classic (the model I own) is discontinued, PYI still services them and sells parts.  I contacted the service department and they got back to me with all the info I needed along with a detailed pdf on assembly.  They even took the time to run Velorum (displacement), along with engine size, and transmission gear ratio to give me a recommended pitch setting for the prop.  

Putting it back together was pretty straightforward given how precise everything needs to be in order to have a smooth, balanced, and powerful propeller.  It's really a lovely piece of kit and the engineering is downright elegant. It's simplicity is deceiving, it really has a difficult job in a very unforgiving environment.  Once I got it back together for a test fit (once it goes back on the boat it will be stuffed with grease like a turkey), it looked amazing and operated smoothly.  I was told by support that it should have a tiny amount of play, but more than an 1/8" and I should think about a rebuild.  Fortunately, everything checked out and it's in remarkably good condition.  I don't know the history of this prop, but it should last me for some time as long as I keep the internals greased every year and don't back it over a rock :)



 


Sunday, March 3, 2024

Rattle Can Rebuild Part X

I decided that I wouldn't subject people to any more engine rebuild updates until it was finished, but even though I was technically finished last week, it turns out I wasn't.  I won't go through all the gory details of the final pieces of the rebuild, but I will say that I thought it was going better than I expected.  I picked away at it almost every day since the last time I posted, focusing on each system individually.  By far the biggest challenge was figuring out the new wiring harness, sensors and a new low pressure fuel pump that was not a westerbeke product, but with a little advice from Hansen Marine Engineering, I got it all done.

With everything back together and after lots of electrical testing, it was time to fire it up.  I wired up the battery to the starter solenoid, plugged in the new Admiral panel and oil/water alarm harness and got a bucket of water to run through the raw water pump.  I turned the key and hit the preheat button for 10 seconds to fire up the glow plugs and then pressed the start button.  The engine cranked and cranked, but wouldn't catch.  I stopped and re-checked everything and repeated the process.  Still nothing. The engine cranked fine, but wouldn't catch.  

First I tested that the glow plugs were working; they were. Then I moved onto the only other possibility: the fuel system.  I knew that fuel was making it through the low pressure pump and into the secondary filter and to the injection pump.  However, when I cracked the fuel line at one of the injectors, I found no fuel...  It appeared that the injection pump wasn't working properly, but I spent a day or two scouring online forums to definitively prove that the injection pump was the problem.  I found my answer quickly on the Cruisers Forum where one of the users (SkipperPete) gave me the answer I needed. Yes it was more than likely the injection pump.

During the rebuild, I studiously avoided the injection pump because I naively hoped that it would run after 10 years sitting without running and with old fuel in it.  An additional problem with the injection pump is that it is difficult to get at and in order to remove it, you have to disconnect a very fiddly spring and tie rod that attaches the govenor to the rack on the pump.  I honestly thought it was 'above my paygrade' and seriously considered putting the engine on a trailer and taking it to a diesel repair shop.

I'm glad I didn't and the help I got from the Cruisers Forum gave me the courage to tackle the project. I did have to disassemble the entire fuel system surrounding the injection pump to get at it, but at this point I was sure that I could reassemble it again without too much trouble (but I took lots of photos). However, in the end, pulling the injection pump wasn't actually that bad and I probably saved at least $500 just in the disassembly process.  Now I have the pump out of the engine and will take it to a injection pump shop to have it rebuilt. Yes, this will be expensive, but this is something that is not for amatuers and requires specialized high pressure testing equipment and expertise that I just don't have.  

So tomorrow morning, I'll be dropping it off at Diesels Fuel Injection shop to have them rebuild the pump.  I used them to rebuild the injectors (which also require specialized equipment).  Hopefully, my next post will include a video of the engine running.  Below are a few shots of the injection pump:





Monday, January 15, 2024

Rattle Can Rebuild Part 5

Since the end of August until late December, I had been singularly focused on boat projects, but over the holidays, I decided that I needed a bit of a break. I tend to get hyperfocused on projects and everything else falls by the wayside, but I was on schedule for the engine rebuild so it was time to shut the project down for a few weeks.  I'm glad I did, I really needed a break but didn't realize it at the time.

Now that I'm back I was able to tackle one of the bigger projects of the build and hopefully will be about as deep as I go on this motor.  When doing the initial inspection and research on the engine, I noticed a bit of oil staining on the bell housing underneath the flywheel. After a bit of googling on the usual forums, all signs indicated that it was a problem with the rear main seal.  


 










The oily liquid in the photo is mostly from PB Blaster that I was using to free up bolts on the damper plate, but the black oily residue on the bell housing is coming from behind the flywheel.  I know that these old diesels tend to leak a fair amount of oil, but since I had a rear main seal on hand, I decided it was worth tackling the problem.  

In theory, it's a very simple process, but this task was quite the struggle.  First of all, I had to take it off the stand (it bolts onto the bell housing).  I lowered the engine down onto the rolling cradle to secure it before removing the damper plate (this connects the the transmission and dampens shock loads from the transmission to the crankshaft and vice versa).  This part was straight forward, remove 5 allen bolts and it pulled right off. I was really amazed that I didn't strip or break them off because they were very tight.  This is where things got difficult.  With the damper plate off, the bolts that fix the flywheel to the crankshaft were exposed.  They weren't rusty or corroded, but quite dry and Very tight.  Initially I tried the 19mm bolts with a standard 1/2" drive socket wrench and couldn't budge any of them.  Next I tried my cordless impact wrench.  Nothing.  Finally, I slathered multiple coatings of PB Blaster on each bolt and called it a day.

The next day I tried a 2 foot breaker bar and while I did crack one of the bolts, I was starting to strip the heads on several of them... Time to rethink my strategy or I'd be in for a lot of trouble.  I finally dug out my old compressed air impact wrench and fired up my 33 gallon compressor.  At the wrench's 90 psi maximum rating I got the same result as with the electic impact wrench, which is to say: nothing.  I decided to go for broke and turn the psi up to 140.  I figured it would probably blow the seals on the wrench, but incredibly it actually wor ked and I didn't break a single bolt.  All that banging on the bolts also freed up the flywheel from the cranshaft and it came right off the flange.  All my reading up until that point lead me to believe that the flywheel was going to be stuck hard onto the crankshaft and would need a solid beating to get it off.  

With the flywheel off, I had to lift the engine again with the chain hoist and then unbolt the bell housing before lowering it down onto wood blocks (the bell housing is cast with 2 of the 3 engine mount brackets, so when it comes off, the engine has to be supported another way).  Technically, I could have replaced the rear main seal without removing the bell housing, but I wanted to replace the gasket between the engine and bell housing so it had to get pulled. I degreased and cleaned it all up before priming and painting it. Once the paint dried, I put a thin layer of permatex #2, re-gasket'd it and set it aside until the main seal was replaced.  

Replacing the main seal was pretty straight forward. The seal is held on the crankshaft with an aluminum housing and the bolts holding that to the block came off without issue.  With the housing and seal off, I inspected the crankshaft surface and it appeared to have some minor scoring marks on the surface where the seal was.  I installed a shaft sleave (a thin ring of metal, interference fit), but realized that the flywheel wouldn't go back on with it in place so I had to cut it off.  Hopefully the scoring in the crankshaft won't cause the new seal to leak, but I'm not going to pull the whole crankshaft (it would require a full engine teardown, and I'm not going there).  So I just pressed the seal into the housing and then slid it over the crankshaft and bolted the housing back in place (along with a new housing gasket).  

I re-installed the bell housing and with the help of my son, we wrestled the flywheel back in place and bolted it on with the new OEM bolts I ordered. I wasn't going to re-use the original bolts after the beating they took getting them off. Finally, I bolted the damper plate back on and called it a day. Time will tell if the seal still leaks, but it will be better than before.