One of the big problems with boat refits when you are doing everything yourself is the fact that most jobs require very specific parts that need to be ordered in advance and can take time to arrive. Additionally, most of these jobs often require very a different set of skills and will often need a fair amount of research if I haven't done the job before. This research often requires me to totally disassemble a piece of equipment so that I fully understand it before moving forward. As a result, I often have 2-4 jobs underway simultaneously and my brain and workspaces can get pretty messy.
Such is the case with the roller furling unit. Specifically a Profurl P-40 that was likely original equipment on the boat. When the boat was purchased by the previous owner, the sea trail survey indicated that the furling equipment was in good condition and fully functional, but that was over 10 years ago and the furler has been sitting in a yard ever since. I really didn't want to shell out $3k+ for a new furling unit so I set out to assess its condition after sitting so long.
I knew that this particular furler has been out of production since the late 80s but everything I've read indicated that they were solid units with a long service life and could be repaired. It wasn't until I stumbled upon a youtube video (
here) of someone restoring an old Profurl (not the same model as mine) that I thought that I might be able to actually re-use it. The youtube channel is Living For Sail and the person producing the videos is an engineer with a bigger project than mine and has a lot of great videos.
Profurl is now owned by a different company than when the unit I have was produced so they have zero information (or parts), but the Living for Sail video gave me hope that I would be able to replace the seals and bearings in my unit with off the shelf industrial parts. This is one of those cases where the research requires a complete tear down of the equipment to fully assess what and how it needs to be done.
The biggest problem I could see with it was that the furling drum (injection molded nylon?) was not in great shape and had a lot of UV degradation from sitting in the sun so long. As luck would have it, I happened upon a craigslist ad for an old profurl furling unit. The owner had purchased it off ebay thinking it was a different model (LC42) to use for parts on his unit, but looking at the photos I could see that it was exactly the same as mine. I contacted the seller and after he sent me a few more photos I was sure that it was a P-40 and the furling drum appeared to be in much better shape than mine. I bought it for $110USD shipped.
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Upside down core |
Now that I had a decent furling drum I dove deeper into the unit and set about to remove the bearing(s). I didn't know it when I started, but the Living for Sail video was a much larger unit than mine and had multiple bearings and dreaded circlips but the process was the same. I pulled off the furling drum to reveal the core of the unit which is 2 machined aluminum cylinders. The smaller diameter cylinder attaches to the foil (and sail) and rides on the bearing of the outer cylinder that is attached to the deck. This provides the rotating surface for the sail to furl.
To get at the bearing and see what's happening inside, I needed to remove an oil seal on the bottom of the unit. This proved to be very tricky. You can't just pry it out because the seal is an interference fit and while I originally thought it was rubber, it turned out to be rubber coated steel. So, following the Living for Sail video, I drilled into it with some construction screws and tried to remove it with some vice grips: No dice. Next, I pulled out the trusty 2lb slide hammer and was able to finally get it out after drilling more construction screws in at various points in the seal.

With the seal out, I was able to see into the unit and find that there was only one bearing and 2 circlips. Using a pair of 9" circlip pliers I removed the outer circlip, taking care not to score the aluminum walls of the cylinder that would make re-sealing the unit difficult. If you ever do this, make sure you wear protective gear because the circlips are made of spring steel and they are scary. They are under a ton of tension and if they slip out of the pliers they fly and are pretty sharp. After the outer circlip, I did the same with the inner circlip that holds the inner cylinder in place. Same deal, be careful.
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These things can be very mean!
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With both the circlips out, I 3d printed a 'press' to knock the inner cylinder out from inside the inner bearing race. This was fairly straightforward, I printed the press to be about 1mm less than the diameter of the inner cylinder and then supported the outer cylinder with a few blocks of wood and pounded out the inner cylinder with the press and a hammer.
With the inner cylinder removed, I turned over the outer cylinder and tapped out the bearing and the top oil seal with a block of wood. Both came out with surprisingly little fuss.
At this point I was able to confirm that the bearing and oil seal sizes were as follows:
1. Bearing - 50x80x10 (I ordered a sealed bearing)
2. Top Oil Seal - 50x76x12 double lip w/ spring
3. Bottom Oil Seal 50x80x13 double lip w/ spring
As far as I can tell, all the Profurl units of this vintage (80s-90s) are using the same bearing size and probably the same seals as well. The good news is that these bearings and seals are easily found on Amazon or Grainger or McMaster and are used in tons of industrial applications so they generally hold up well. I ordered everything through Amazon and 2 days later they were at my doorstep.
I put the bearings in the freezer and then cleaned up the aluminum cylinders of old grease and dirt. To be honest, I had hoped they would polish up a bit better, but once reassembled, it should be functional for many more years. Once satisfied that they were at least clean (but not pretty), I turned over the larger of the 2 cylinders and greased up the small oil seal (will be the top of the furler just under the drum) and pressed it in. It was another interference fit, but I warmed up the cylinder to 180 degrees F and with the grease it slid right in place with a little tapping with a block.
For the bearing, I 3d printed another press (diameter 79 mm to support the outer race or bearing surface). Worried that I would melt the plastic coating on the oil seal already installed, I just relied on the shrinkage of the cold bearing and more grease. With the bearing press and some gentle taps of a hammer it dropped in without any issues. Speaking of grease, I used Lubriplate 130AA lithium grease (for the MaxProp) for all the internals.
While the bearing was still cold, I carefully re-installed the large circlip to keep the bearing in place and then using a 2" piece of pvc pipe to support the inner race of the bearing, I flipped the large cylinder back over and tapped the smaller cylinder through the center of the bearing. With that seated, I installed the remaining circlip, packed the whole thing with grease and pressed the large oil seal into place.
Everything else was simple, just a matter of re-installing the drum, cage, and mounting plates to the bottom of the furler and it was whole again. It was definitely a tricky job that required patience, but anyone who is a bit mechanically inclined should have no problem doing this. The hardest part was the circlips, definitely get a good pair of 9" circlip pliers.